Timed

Now that the wasps are dead I can get to reinstalling my timing belt. There are already a number of good videos on the subject, so I won’t bother to reexplain the procedure here, but a few notes from my experience.

  1. Don’t try to move the cam gear with your hand. Unlike the intermediate gear it’s very stiff. I ended up momentarily bending my thumb a weird way while trying to nudge it a bit, and while not damaged it’s now irritatingly sore.
  2. The crank gear is relatively easy to move once the pulley is on. Larger moves require a breaker bar with a 24mm socket on the bolt.
  3. Once all three are lined up properly getting the belt on might require some playing around with the tensioner. Mine needed to be compressed just a little but more than it was with the nail I was using to keep the spring compressed. I need to use one hand to lever the spring another 1/8 of an inch or so while pushing the belt onto the roller all while keeping it from slipping off the other gears.

To be honest, the whole affair was a bit more of a pain that I imagined it would be. I actually had to sort of back away at one point and take a break lest my frustration end in something breaking. Working while keyed up by frustration is a sure fire recipe for disaster. Anyway, everything is lined up and the new belt is on, so progress.

Natural Complications

I’ve been away for about a week on holiday with my family, but towards the end of the trip my Volvo began to creep back into my mind. now that the missing timing belt cover had come in, I was very eager to start putting the engine back together. When I finally got home I had an extra “recovery” day, and I had planned to spend at least part of it starting that process.

Mother Nature had other ideas.

While I was away a bunch of damned, dirty wasps had decided to make a house right above my car. That made working a little bit precarious. Looking up the correct method of wasp killing, I found that the best time to attack the nest was at dusk. So much for my planned day of work, I guess!

Come dusk I came out with my can of poison, blasted the nest, and ran like hell. I returned a few more times to make sure the job was done, and I’m happy to say that the next day on (today) there is little to no activity around the nest. I think I’ll get more poison to make sure the whole thing is inhospitable to wasp life as possible and then cut the branch out and dispose of the nest. Then I can get back to business.

Bulb Mania

So far I’ve had to replace almost every light bulb in my car. From that experience I can vouch for how confusing and surprisingly expensive that process can be. I wish I had seen this post on Matthew’s Volvo Site before today. In it user “QuirkySwede” breaks down the most common bulbs found in Volvo cars plus the various designations given to them by Volvo, Sylvania, Osram, and the other parties involved in manufacturing or selling these bulbs and provides tips on which to use and when.

Summer weather

Not much work has gotten done in the last week, and there is a reason. Two, actually. The first was that the back plate to my timing belt cover decided to spontaneously self destruct after I took it off. The two front pieces are still in relatively good shape, but the back piece was hopeless. I had to order a replacement set, and that was back ordered at iPd so it took a little show up. It has, in fact, shown up, but Mother Nature decided that we had been become spoiled with mild weather in the last month. This past weekend was in the triple digits. I am not a hot weather person in any way, shape, or form. That put a stop to my plans on reinstalling the timing belt, water pump, and accessory belts, but I assure you that as soon as the weather decides to cooperate I will be back at it. In the meantime enjoy a couple of pictures featuring my melted back cover and a side-by-side of the old and new covers complete with reproduction decal!

Timing belt and water pump

In the week since my last post, I’ve continued to tear down the front of the block. This includes the cam and intermediate pulleys, timing belt, and perhaps most dramatically the water pump. I did the pump first mostly to get it out of the way of the timing belt tensioner (part #463633) and the timing belt itself. I also wanted to make sure the bearing were still good. Unbolting it was straightforward, but the gasket was pretty well stuck to the block and required some scraping and peeling to get it off.

The pump seems fine. It doesn’t rattle and turns smoothly, but there was an alarming amount of crud inside of it. I’m not sure what it was – perhaps just dirt or more likely antifreeze that has crystalized over the years. I washed it out and set the pump aside for cleaning. Also, on the advice of a friend who has experience with 240s, I replaced the thermostat. There didn’t seem to be anything wrong with the existing one but since I was in there I figured it was as good a time as any.

Next I wanted to get the timing belt off. The first step was to loosen the bolt on the tensioner pulley and, using channel locks, compress the spring. This part was easy and allowed me to slip the belt off relatively easily. It wasn’t in terrible shape, to be honest, but the belt change sticker that was on the timing belt cover had no discernible date written on it, so I figured since I was changing all the other belts I should do this one too. I also wanted to take the cam timing and intermediate gears off to better clean them up. Do do this you need to keep both the cam and intermediate shafts from turning which it is wont to do if it’s not arrested by the timing belt itself. I accomplished this by first hitting the bolt with lots of WD-40 to loosen it up a bit. Then I took the old timing belt and fitted it to the gear, wrapped it around the tensioner peg, and used locking pliers to keep it on. This gave me the leverage to get both gears off.

Next step is to clean the front of the block up with some degreaser and WD-40, clean the gears, de-crud the water pump and replace the rubber seals, and put it all back together.

Getting into it now

My replacement ECT sensor arrived. The time has arrived to really get serious about cleaning and reassembling this engine. First (obviously) comes the disassembly part. I’ve already got the intake section off. Next on the list was the various belts. Well, maybe the second thing. The first hing I did was put the ECT and temperature gauge sender back in and reconnect them.

Back into the block
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Part numbers

My new Bosch brand ECT sensor has arrived from iPd, so I thought I’d take a moment to talk about part numbers for anyone reading who may also want to replace this part but not know which one to get specifically.

Volvo has part numbers assigned to almost ever piece that goes into their cars. However not every part is actually made by Volvo. Parts that are shared across not only Volvo’s but other company’s cars are usually made by third parties called “original equipment manufacturers” or OEMs. In Volvo’s case, one of the biggest OEMs is Bosch, a German manufacturer of, well, lots of things. Bosch also has a part number for their own products separate from those assigned by the companies that buy from them.

In my case, Volvo’s number for the ECT sensor used in my particular model and year of Volvo is 1346030. Bosch originally numbered this part as 0280130032. However, at some point Bosch decided to renumber this part as 0280130069. Why? I have no idea, but it did leave me scratching my head a little until I gathered enough evidence from the internet to confirm that this is the case.

So I now have a Bosch 0280130069/Volvo 1346030 ECT sensor to replace the FAE 33090 sensor that probably replaced the original Bosch 0280130032.

Crystal clear.

Engine coolant temperature sensor issues

Today I attempted to test my ECT sensor. The procedure went like this:

  1. Boil some water
  2. Connect my multimeter up to the sensor
  3. Dip the sensor into the water and take occasional temperature readings. Compare the resistance readings to the temperature to see if they should be where they are expected

I did all this and got wildly unexpected results. Way higher resistance than I expected. For reference, here is the chart showing what I should have seen.

Part # 1346030

Looking at the sensor I noticed that it actually wasn’t Bosch branded. It was made by Spanish manufacturer Francisco Albero S.A.U (aka FAE). I’m not sure that company was ever an OEM supplier to Volvo, so I’m sort of suspecting that this sensor had been replaced at some point and that the not so good FAE replacement has since failed. Regardless, I have a Bosch replacement on the way. Since this thing is such a pain to access I want a good part going in before I reattach the intake manifold.

Injectors are back

After disassembling the intake manifold I was left with four loose and very dirty looking fuel injectors. I had originally intended to clean them myself, but in a moment of startling honesty I admitted that I’d more than likely either ruin them or not really clean them very much. So I looked around the internet and decided to turn this job over to the aptly named Mr. Injector. Unlike me, he has both the experience and the equipment to do this right, and his prices aren’t terrible especially when compared to having to buy new injectors because I broke one in my own half-assed attempt at fixing it. So I boxed them up and sent them off to Idaho.

His site told me that I’d be getting a baseline electrical, spray pattern, leak, and flow test followed by disassembly of the “soft” parts, an  ultrasonic bath, a flush for contaminates, and finally a new set of tests to measure the improvement in function. Then they’d be oiled, have their soft bits replaced, and finally repainted with corrosion resistant paint. About a week from when I sent them they arrived back at my house and I must say I am very impressed.

As you can see they’re obviously much cleaner looking, and the flow test suggests they’re much cleaner on the inside as well. Interestingly, one of the injectors was still in very good condition while another was merely in fair shape. Overall they were still functioning quite well, but I’m glad to know that they’re now in tip top shape with new filters and pintle caps. And he also sent me candy! That’s service.

MAF: Good

This past weekend was a bit of a bust in terms of car work. Aside from several obligations, a big tree branch broke off and fell onto the roof of my garage. I did have a moment the other day to put the multimeter onto my MAF sensor to what I could see. According to my intake system green book, the MAF should show a resistance reading of between 2.5 and 4 Ohms between pins two and three, and mine was reading somewhere around 3 Ohms. A visual inspection shows the wires still intact, and I’m assuming it’s clean because I had already cleaned it many months ago and haven’t really driven since then. So, I’m willing to move this part into the “working” pile along with the IAC. Stay tuned to see if the two engine temperature sensors can go there too.

Volvo announces ‘Tow For Life’

Photo Credit: rat_fink (flickr)

Volvo will tow any Volvo in the world. For free. Have a new V90? They’ll tow it. A PV444 from the 50s? It’s getting towed! My ’92 240? SO TOWED, YOU GUYS!

Car and Driver reports

No matter what Volvo passenger vehicle you own, no matter how old it is or how clapped out it might be, it now qualifies for free roadside towing. Volvo is extending the free towing service it provides in-warranty customers via its roadside assistance coverage to every Volvo model, “no matter what vintage,” according to the automaker, which has dubbed the service Tow for Life.

Good on Volvo for not completely forgetting their older cars. I hope I never have to use this service.

Testing the IAC Valve

The Idle Air Control valve, commonly just called the IAC, is a servo motor controlled valve that helps maintain the engine at idle according to the demands of the engine control unit (ECU). Given that my engine was having a hard time idling for more than a few seconds a failure here would not be surprising. I had already taken it off, so I figured I’d get it on my workbench and poke it a little to make sure it’s still working as expected.

Testing Procedure

The IAC is a pretty simple device. It’s a tube with a servo motor inside that opens and closes a valve to control airflow into the intake manifold. How far open the valve is depends on the voltage supplied. 12 VDC should open the valve up all the way. I also referenced the Volvo “green book” on the intake system and found that the resistance across the two input terminals should be 8 Ohms. So those are the two tests I performed. I’m happy to report that my IAC is just fine. It wasn’t difficult to test, but just in case here’s a video to illustrate how I did it.

Off-taking the Intake

So it’s been a year or so since I bought this Volvo. When I first took it home it (obviously) drove, but not well and would probably not pass inspection. It was a project from day one. Now that better weather has arrived, I’m determined to get the car running reliably well and road worthy. At that point I can pivot to making sure the rest of the car is good.

So, given a day with a few hours free my oldest son and I began taking off the intake system. These parts include (starting from the out and moving in):

  • The air box and filter
  • The mass airflow sensor (MAF)
  • The throttle body
  • The intake manifold
  • The idle air control valve (IAC)
  • The fuel rail, fuel pressure regulator, and fuel injectors
  • The engine coolant temperature, engine temperature gauge sender, and knock sensors

The plan was to first drain the coolant system and remove the radiator and fan to provide some working room and then start removing the above listed parts. They would then be cleaned and tested for function before being either replaced or put back on.

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On rear window nozzles

In the course of replacing the gate wiring harnesses I also had to disconnect the rear window washer nozzle. The nipple over which the fluid hose connects is actually inside the gate. This meant that I had to remove the nozzle in order to reconnect the hose. I Googled around for instructions on how to do this and found a number of people also asking the same question but no real answer. So for the benefit of the internet, I bit the bullet and tried to do it myself.

From memory (and photos of the part I found online) I knew the nozzle was kept in place by plastic tabs. This meant that they probably would be flexible enough to be removed, maybe even without breaking! I selected a plastic trim removal tool with a notch in the end and worked it down around the stem of the nozzle where it entered the gate.When I felt that I had pushed it down as far as possible I levered the tool back. After a bit of tentative attempts I finally used enough force and the nozzle popped off, thankfully still intact.

The anatomy of a washer nozzle

As the photo shows, the nozzle is actually a three part assembly. There is the main section, the part that actually attaches to the gate and provides a fitting for the fluid hose, the outer housing that provides a small slit that constricts the flow of washer fluid and creates the spray, and a foam gasket that helps keep water and other liquids from entering the inside of the gate. You might notice that my foam gasket has ripped a little, probably a result of the levering action required to remove it from the gate. This is probably unavoidable unless you’re super careful as the section of foam that ripped it quite narrow. Perhaps inserting the tool from the bottom might have worked better. Anyway, I might be able to fix it with a dab of rubber cement or I could cut a new one from the neoprene I used to rebuild the air box gasket.

A half-useful weekend

After a long while, the weather decided to cooperate and be pleasant on a weekend day where I had some free time. So I decided to tackle the rear wiring harnesses.

Disassembly

Armed with instructions I had downloaded from our friends at iPd, I dove in. The first thing that needed doing was detaching of the headliner in the rear. I had previous dithered on this because my initial meek attempts at removal were unfruitful. It turns out that this was because I was following the instructions too closely and attempting to remove the liner with just my fingers. I had purchased a set of hooks and probes awhile back for a different purpose and decided to see if they helped. Indeed they did! Using a hook the headliner peeled back perfectly and with almost no effort. I was in! The next step was to star loosening the retaining bolts. On my car these consisted of two bolts that held the hinges to the body and two large screws that held them to the tailgate. With the help of my older son, who was gracious enough to climb inside and actually remove the fasteners while I held the tailgate to keep it from falling, we got them all out and lifted the gate from the back of the car.

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